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Locomotive to
Tender, Detensioning & Uncoupling |
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Due to lack of space we need to uncouple the tender from the locomotive
and move it backwards in order to remove the locomotive cab for major
repairs. And it is possible that for the big move we will move the
tender and locomotive separately, even though we will be towing them on
track and ties. |
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Tensioning and
Coupling Devices
The locomotive in on the left; the tender on the right. In the
bottom 1/3 of the photo is the drawbar. It comes out of the
locomotive horizontal, bends upwards, and horizontally enters the
tender.
The upper 2/3 thirds of the photo is the tensioning device. It
consists of a bumper which contacts a pad on the locomotive. The
bumper is pushed towards the locomotive by a wedge. This wedge is
kept pushed in by a spring loaded rod mounted to the leading edge of the
tender. |
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Looking at the drawbar and tensioning device from the engineer's side.
Note the wedge is only about 1/2 inch thick on this side. |
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Another shot from the fireman's side but a little lower prespective. |
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Our locomotive is coupled to its tender with a drawbar. This
drawbar is very important. Every car being pulled by the
locomotive is being pulled with that drawbar.
That drawbar fits into a pocket in both the tender and the locomotive.
Each end is then held in place with a large vertical pin. One end
of the draw bar is pinned to the locomotive and the other end to the
tender. Safety retaining straps go
through the bottom of pins. This stops them from
working up and the tender becoming uncoupled.
To keep the tender to locomotive distance constant, a tensioning device
is used. Most are spring loaded bumpers. To uncouple the
tender, one needs to push the tender forward, compress the tensioning
device, remove the safety retaining pins from one of the big vertical
pins, move the big vertical pin upwards which will release one end of
the drawbar. When the forward pressure is release from the rear of
the tender, it will move backwards and the two will be uncoupled.
If life were only that simple!
Our tensioning device is not a spring loaded bumper. Our bumper is
pushed forward in by a spring loaded wedge. It might have moved
freely at one time in its life. Today it is rusted in place,
probably micro welded by high amounts of friction, and grooves formed in
each the pieces that should be moving. |
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We had tried to hammer the wedge
out, using both the faithful ol' sledge and an electric.
And of course
there was lots of penetrating oil. We
tried a puller that we had made along with more hammering and penetrating
oil. |
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Mark Haire tries to loosen the wedge with a sledge. |
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Mike Stuckert prepares an electric hammer. |
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Finally, on our May 7th work session the tender was detensioned
from the locomotive. We tackled the problem from four
directions.
1. We jacked up the bumper.
It appeared to be canted downwards. We thought this would break
some rust free and possibly relieve pressure between the
bumper and the wedge. At least it would change the interfacing
surface positions relative to each other.
2. We pushed on the wedge.
We obtained a porta-power, basically a long hydraulic sleeve with
versatile fittings and extensions. We jacked against the 1/2 inch
facing of the wedge using the tender frame as a base.
3. We obtained a heavier sledge
hammer with a longer handle.
Jacking up the bumper was a good idea. The small jack we brought
was still too big so we diverted the porta-power to this task.
That worked well. We had to jack the bumper up on one side, stuff
metal tool handles under that side and jack up the other side to get
both sides up at once. We couldn't jack the middle of it because
the drawbar was there.
We tried pushing on the wedge using the porta-power. That wasn't successful........ until.........
We noticed the wedge had about 3/4 inch of
room to move upwards. So we obtained a 30 Ton hydraulic jack from
our local rental supply (who, by the way, lets us use the equipment for
free on this project - Thank you, Great Plains
Rentals!) We alternately jacked up the wide end and then
the narrow end of the wedge and knocked them back down with the sledge.
After removing loosened rust we repeated the process until we could
knock the end of the wedge up and down using a small hand sledge.
After that the porta-power began to move
the wedge. When we ran out of throw on the porta-power we used the sledge. Finally after several work sessions with no luck, the wedge was sitting
on the ground. That is one solid, heavy piece of metal. |
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The porta-power
pushing on the narrow edge of the wedge. |
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The 'wedge'
finally removed. |
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The gap between
the bumper and the locomotive. |
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Uncoupled
- March 21, 2009
On March 21, we uncoupled the tender from the locomotive.
All I want to say to anyone getting ready to work on an old rusted steam
locomotive without the benefit of a well equipped shop: Try
anything and everything until you get it done. When you
begin any effort, you'll never know exactly what all the conditions are
with which you will be working. When you complete your effort, it
will be pretty obvious what you really should have done. Until you
get to that point, prioritize the suggestions, but don't discard
completely any suggestion. Of course, SAFETY has to be the number
one priority in everything that is attempted. |
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Here is a prime example:
We were sure the drawbar pins
were in a bind and we hadn't been able to move the tender forward with
the 'car mover'. We decided that this might be caused by the
tender being empty and riding higher on it's springs that normal - thus
the drawbar might be cocked.
While we would have liked to add
weight by using water bladders or bricks, all we had at our disposal
right then were people. We only had five people (including the
photo taker) who weren't needed below and had the ability to climb into
the tender. And of those five, three don't add up to much weight
wise.
We didn't really think this would change
anything. It only cost us 10 or 15 minutes. And yes, we did
try jumping up and down all at the same time. (it didn't help at
all) |
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Our plan was to move the tender forward with this Power King car mover
supplied to this project by Advance Carmover Company. Even though
we had cleaned and lubed the tender axles, they are friction bearings
and didn't move that easily. Actually the wheels were raising off
the rail instead of the car moving. The Carmover has a lot of
mechanical advantage.
After a couple hours one of our workers got
the tender to rock forwards about 3/4 inch. |
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Once we realized the tender and drawbar
were moving back and forth as one with respect to the tender, we began
working on the tender pin. We jammed a rail spike under the back
of one of the tender wheels and hammered it in as the tender was being
rocked. By this manner we gained an inch. At this point, the
jack began moving the pin upwards. Within minutes it was able to
be extracted by hand. |
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Above: Our newest member, John McDevitt, removes the loosened pin
by hand. It's a pretty cramped space under the locomotive cab.
Right: the pin with its keeper. It is 21.5 inches long and
3.5 inches in diameter. The bottom 2 7/8 inches is 2.5 inches in
diameter. It probably weighs 50 pounds. |
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